A door panel that <a href="https://www.thenationalnews.com/business/aviation/2024/01/14/alaska-airlines-to-widen-quality-checks-on-boeing-737-max-9-planes/" target="_blank">flew off a Boeing 737 Max 9 jet mid-flight</a> on January 5 appeared to be missing four key bolts, according to an initial report by a US safety board investigating the incident. Photo evidence released on Tuesday shows bolts were missing from the door plug, which had been removed to fix rivets that were damaged in the production process, according to the independent US National Transportation Safety Board report. Until now, the NTSB had not said what caused the panel to rip off an Alaska Airlines-operated jet as the plane climbed to 16,000 feet after taking off from Portland, Oregon. The incident has become a full-blown safety and reputational crisis for <a href="https://www.thenationalnews.com/business/aviation/2024/01/10/boeing-ceo-max-737-plane/" target="_blank">Boeing</a> that will slow plane production and risks it ceding further market share to rival Airbus. The US Federal Aviation Administration <a href="https://www.thenationalnews.com/world/us-news/2024/01/06/alaska-airlines-grounds-boeing-737-max-9-planes-after-window-blows-out/" target="_blank">grounded 171 of the Boeing 737 Max 9 planes</a> after the incident, most operated by US airlines United and Alaska Airlines, for inspections. Those planes were cleared to return to service in late January. The NTSB has been focused on how the panel – fitted into this Max 9 model in place of an optional exit – detached from the plane. The plug is held down by four bolts and then secured by “stop fittings” at 12 different locations along the side of the plug and the door frame. All 12 stop fittings became disengaged during the event, the NTSB said in January. Both United Airlines and Alaska Air said in the days after the blowout that they had <a href="https://www.thenationalnews.com/business/2024/01/08/united-airlines-finds-loose-bolts-in-boeing-737-max-jets-during-inspections/" target="_blank">found loose parts on several grounded Max 9 aircraft</a>. The plug was manufactured by Spirit AeroSystems, the onetime subsidiary of Boeing that separated from its parent in 2005. The production process involves work at both its Wichita, Kansas, facility before plane bodies are railed to Boeing's Renton, Washington, plant. The FAA has taken a harder line than in the past on Boeing. In late January, it barred Boeing from expanding production of its 737 Max planes due to the quality issues. That means it can continue producing Max jets at its current rate, but it cannot increase that rate. “I certainly agree that the current system is not working, because it's not delivering safe aircraft,” FAA administrator Mike Whitaker told Congress on Tuesday. “So we have to make changes to that.” The FAA is conducting an audit of 737 Max manufacturing, which is looking at all elements of production at Boeing and fuselage production at its supplier Spirit. Boeing shares were up 1.6 per cent in trading Tuesday; the <a href="https://www.thenationalnews.com/business/markets/2024/01/09/boeing-stock/" target="_blank">stock has lost more than 20 per cent of its value</a> since the beginning of the year. Boeing will look at the preliminary results from the NTSB investigation of the 737 Max 9 blowout and decide whether to take more action around the door plug, a Boeing quality official said on Tuesday. "We're going to look at the changes we've already put in place in our factories and other places around the plug specifically," Doug Ackerman, Boeing Commercial Airplanes vice president of supplier quality, said during an aerospace supply chain conference near Seattle. He added if Boeing found it had already made the changes needed to address the specific problems raised by the NTSB investigation, "we're going to look at other places where we need to apply the same rigour".